1 Introduction

In the second half of the 1980s, in the initial phase of the development of the magnets for the Large Hadron Collider (LHC), a crucial issue was the choice of the superconductor. The only industrially available materials at that time were Nb-Ti and Nb3Sn. The former had already been successfully used in large solenoids such as the OMEGA (Morpurgo 1970) and the Big European Bubble Chamber (BEBC) magnets (Haebel and Wittgenstein 1971), in the Intersecting Storage Rings (ISR) superconducting quadrupoles (Billan et al. 1976) at the European Organization for Nuclear Research (CERN), and then massively in the Tevatron (Wilson 1978) and Hadron-Elektron-Ring-Anlage (HERA) (Wolff 1988) particle accelerators. Nevertheless, the field level required for the LHC, between 8 and 10 T, could be reached only by lowering the operating temperature to about 1.9 K, requiring a new cryogenic system, still to be developed.

At that time, Nb3Sn had been used only in a few short model magnets, with mixed success. Its brittleness forbids winding reacted conductor around small curvature radii (about 5 mm for the LHC dipole coils) and, thus obliges that coils are wound with conductors containing precursors of the superconducting compound. The wound coil then has to be submitted to a heat treatment at about 700 °C to form the superconducting phase. This heat treatment step at about 700 °C required the development and use of insulation systems able to withstand this treatment, the construction of a complex tooling to maintain the coil strongly confined in its precise shape during the whole fabrication process, and extreme care in all handling operations after the reaction heat treatment to not damage the brittle superconductor.

In view of the considerable potential of Nb3Sn, notably its high critical current density at the field levels required at 4.2 K, and the higher specific heat and temperature margins as compared to Nb-Ti at 1.9 K, CERN decided to build a 1 m long dipole model using this superconductor. This decision was taken to ensure that the best choice for the LHC would be adopted, although the construction of this Nb3Sn dipole model came with numerous challenges, which had to be overcome. An additional argument to test Nb3Sn technology was the potential need for high-strength quadrupoles in the interaction regions with large apertures and in the presence of increased heat and radiation load.

The strategy for the construction of the Nb3Sn dipole magnet was like that adopted for a Nb-Ti model (Perin et al. 1989), i.e., to design and build the magnet in close collaboration with a qualified industrial partner (Perin 1990). The reason for this approach was twofold: (1) to involve industry in the technological development in order to prepare it for the future production of the LHC magnets; and (2) the clearly insufficient resources available at that time in the CERN laboratory for LHC magnet research and development (R&D), as CERN was heavily committed to the construction of the Large Electron–Positron Collider (LEP).

A CERN delegation paid visits to several European electromechanical companies to invite them to collaborate with CERN in the development of the LHC magnets. Thorough discussions took place with the firms that expressed an interest: ELIN-UNION at Weiz, Austria, was selected as the most suitable for building a short model magnet using Nb3Sn superconductor.

2 The CERN–ELIN Collaboration Agreement

A Collaboration Agreement for the design, manufacture, and testing of a 50 mm aperture, 1 m long single bore dipole model magnet using Nb3Sn conductor was signed in August 1986 with the Austrian company ELIN-UNION.

In summary, the agreement foresaw the following.

  • The design of the magnet and all necessary tooling were to be done at CERN by a common CERN–ELIN team. For this purpose, ELIN, at its own cost, sent to CERN one graduate electromechanical engineer, one production engineer, and one designer, who were integrated into the CERN project team.

  • The superconducting cable was specified, procured, and qualified by CERN and then supplied to ELIN.

  • Manufacturing of tooling, coils, mechanical parts, test assemblies, final assembly of the magnet, and factory tests were ELIN’s responsibility with the assistance of members of the CERN team in the most delicate phases.

  • Final tests were made at the CERN cryogenic laboratory under CERN’s responsibility with the assistance of members of the ELIN team.

  • The dipole magnet remains the property of ELIN.

After the successful conclusion of this project and CERN’s decision to adopt the Nb-Ti line for the LHC magnets, the collaboration of CERN with ELIN continued with the construction of short and long Nb-Ti models until the end of 1994.

3 Magnet Design Concept

The design, construction, and performance of the Nb3Sn 1 m long model magnet are described in Wenger et al. (1989) and Asner et al. (1990). Transverse dimensions, coil cross-section, and the magnetic and mechanical structures were designed to be compatible with the 1985 preliminary design of the two-in-one dipole magnet for the LHC (Hagedorn et al. 1985). A simplified cross-section of the dipole cold mass is shown in Fig. 4.1. The main components are the two layer coils, a set of aluminum alloy (Al-Mg-4.5Mn) collars locked by stainless-steel keys, a laminated iron yoke vertically split in two halves, and an outer aluminum alloy (Al-Mg-4.5Mn) shrinking cylinder. The main parameters of the magnet are summarized in Table 4.1.

Fig. 4.1
figure 1

Simplified cross-section of the magnet: 1 – coil; 2 – coil central post; 3 – collar; 4 – iron yoke; 5 – gap; 6 – shrinking cylinder

Table 4.1 Parameters of the magnet

4 Superconducting Strands and Cables

Each coil consists of two layers composed of insulated Nb3Sn Rutherford-type, keystoned cables having the same width but different thickness to grade the current density to peak field in each of the two layers. The superconducting cables were made from multifilamentary bronze route Nb3Sn wires: their characteristics are reported in Table 4.2. These wires and cables (bronze route) were produced by Vacuumschmelze GmbH, Germany.

Table 4.2 Characteristics of the superconducting cables

Cross-sections of inner and outer coil layer cables are shown in Figs. 4.2 and 4.3. A thin tantalum diffusion barrier (about 4% of the strand cross-section) separates the bronze/Nb/Nb3Sn part from the outer stabilizing copper ring.

Fig. 4.2
figure 2

The inner layer cable’s narrow edge showing strongly deformed strands. (Courtesy of Vacuumschmelze GmbH, Germany)

Fig. 4.3
figure 3

Cross-section of: (a) outer layer cable; and (b) strand. (Courtesy of Vacuumschmelze GmbH, Germany)

Samples, some of which were bent around a 5.5 mm radius before reaction, and a cable-to-cable splice about 125 mm long, were measured at the Fermi National Accelerator Laboratory (FNAL), which was at that time the only place having a suitable test station. No sample could be quenched up to 10.8 T and 19.7 kA at 4.2 K. The contact resistance of the splice measured at this field and current was about 1.25 nΩ.

An early coil (mirror coil), tested in the Mirror Coil Test Facility (see Sect. 4.7), had an inner shell made with a higher Nb3Sn content cable (Cu/non–Cu ratio of 0.22 instead of 0.38).

Cable Ic(B) lines and calculated coil load lines are shown in Fig. 4.4. The cable Ic(B) lines were defined by adding the measured Ic of reacted round strands (not extracted from the cables) and applying a reduction of 2% to take into account the expected degradation in cabling and a further 3% reduction due to degradation in bending around a 5 mm radius. The strand measurements were performed at the Vienna Technical University, Austria. These data showed that the magnet design parameters could be achieved with bronze route Nb3Sn cables.

Fig. 4.4
figure 4

Cable Ic vs. B dependence and computed coil load lines

Considering the limits in current density of the bronze route cables and the difficulty encountered in winding due to their stiffness, CERN with the University of Twente, Netherlands, had promoted the use of the innovative powder-in-tube (PIT) conductor under development by the Energy Research Centre of the Netherlands (ECN) (Hornsveld et al. 1988).

For this purpose, CERN ordered from ECN a small quantity of a pilot production of this conductor. A micrograph of a reacted filament is shown in Fig. 4.5, with voids seen in the core. The critical currents reported in Table 4.2 result from measurements performed at the University of Twente using a superconducting transformer (ten Kate et al. 1989). These high critical currents showed the potential of PIT conductors for the construction of high-field magnets. For particle accelerator magnets, however, considerable development was needed to reduce the filament diameter.

Fig. 4.5
figure 5

Detail of a hexagon in the ECN conductor. (Modified from ten Kate et al. 1989)

5 Magnetic and Mechanical Design

5.1 Magnetic Design

The conductors are arranged around the aperture in blocks separated by copper wedges to approximate the cos-theta current distribution. There are four blocks of conductors in the inner layer and two in the outer. The electromagnetic design started with an analytical approach in two dimensions (Perin 1973, 1995), taking into account the presence of a circular iron screen considered as an equipotential surface (μ = ∞). The coil was subdivided into a number of small circular sectors of uniform current density, and their contribution to the field added up by means of a simple computer program. In this case, the coil cross-section, shown in Fig. 4.6, was determined to eliminate the first higher order multipoles.

Fig. 4.6
figure 6

Coil cross-section model. (Courtesy of ELIN, Austria)

The real iron with its variable permeability was then taken into account, using the MARE (Perin and van der Meer 1967) and POISSON (Halbach and Holsinger 1972) programs, in order to optimize yoke thickness, yoke–coil distance and yoke shape. At intermediate fields of about 7 T the computed ΔB/B0 was within 1 × 10−4 at Rref = 10 mm.

The coil end shapes follow the constant perimeter configuration designed by ELIN using a program based on the Biot–Savart law. The conductor blocks are separated by insulated bronze spacers. The ends of the coil, for a dummy coil made from Cu-Ni cable, are shown in Fig. 4.7. This coil was used to practice coil winding and to test the entire manufacturing process, without wasting superconductors. The Cu-Ni cables had mechanical properties similar to the bronze route cables.

Fig. 4.7
figure 7

View of the ends of inner and outer coil layers after reaction (Cu-Ni dummy). (Courtesy of ELIN, Austria)

5.2 Mechanical Design

A hybrid structure was chosen for retaining the Lorentz forces and providing the necessary compressive pre-stress on the coils (Perin 1986). This was known as a hybrid structure, as it produces a moderate compression at room temperature, to avoid creep of the coil materials, and the higher pre-stress required only under cold conditions. In addition, it greatly reduces the deformation of the coil–collar assembly when the magnet is powered.

The yoke dimension is chosen such that a ~0.5 mm gap between the yoke halves is maintained at room temperature. This gap closes between 150 K and 100 K during cool-down depending on the precise dimensions of the collars and yoke. The outer cylinder is shrink-fitted. Figure 4.1 provides an overview of the parts of the structure.

The ANSYS software program (Swanson Analysis System, USA) was used for the structural analysis for which the Young’s moduli E of the windings had been determined by measurements on reacted and impregnated cable stacks. Measurements up to 100 MPa pressure were performed in azimuthal and radial directions by pressing cable stacks in ad hoc made fixtures. Behavior close to linear was found above 40 MPa. The azimuthal E between 50 MPa and 80 MPa was about 19 GPa for the inner layer cable stacks and about 20 GPa for the outer layer. The radial E, almost equal for the inner and outer layer cable stacks, was about 24 GPa. The computed stresses at the pole and mid-plane of the coil at magnet assembly, cool-down and powering are reported in Fig. 4.8.

Fig. 4.8
figure 8

Computed coil stresses at assembly, cool-down, and at 10 T bore field. (Courtesy of F. Zerobin)

Results of measurements on Nb3Sn strands and cables, available when the magnet was built, indicated a strong degradation of current density under transverse compression. For this reason, the pre-compression on the coil was limited to the minimum level to maintain contact at the interface with the central post in all operating conditions. Only 2 years later, new measurements made on assemblies of samples of the magnet cables reacted and epoxy-resin impregnated as in the magnet, showed much smaller reversible degradation (Bona et al. 1991): at B = 10 T less than 2% and about 4% under transverse compressions of 100 MPa and 150 MPa, respectively; at B = 11.5 T, 4% and 6% under the abovementioned compressions. This would have allowed a higher coil pre-compression of up to 150 MPa, which was the testing limit.

The axial Lorentz forces are taken at the coil ends by thick stainless-steel plates bolted to eight tie-rods passing through holes in the yoke.

6 Coil Manufacture and Magnet Assembly

The main components of a coil layer are:

  • A central post, made of copper;

  • Superconducting cables and their insulation;

  • Longitudinal copper wedges;

  • End spacers made of bronze.

A precise winding machine (Fig. 4.9) and sophisticated tooling were designed and built by ELIN, to shape the conductors and hold them in place during winding and the subsequent fabrication phases, since the bronze content made the conductors stiff and springy. This stiff and springy conductor required robust tools capable of applying large forces. No separate heat treatment mold was used, and therefore a part of the tooling used during winding had to be able to withstand the high temperature during reaction heat treatment for several hours. Stainless steel was the material generally used for various tooling.

Fig. 4.9
figure 9

Coil winding machine. (Courtesy of ELIN, Austria)

The inter-turn insulation was made of half-overlapped 0.12 mm thick, 15 mm wide mica-glass tape (Cablosam® 366.21–10, Von Roll Isolawerke, Switzerland). This tape is composed of mica paper backed on one side by woven glass, and is entirely pre-impregnated with a flexible silicon elastomer. To ensure sufficient mechanical stability of the tiny mica flakes after firing of the organic elastomer, the tape was wound with the mica placed on the cable side, so that the external glass fiber (the mechanically stronger component) would maintain them in place and compress them against the cable. The same type of insulation tape was employed for the central post, the copper wedges, and the spacers at the coil ends.

The insulated wedges and end spacers were inserted during winding at the foreseen places. The end spacers were manufactured by casting and milling from bronze. The rough shape was obtained by casting. The final profile was made by inclining the milling cutter of a pre-determined angle and synchronically controlling the advance and rotation of the piece. Edges and corners were carefully rounded off to safeguard the insulation. An improvement of the insulation was tried by flame-spraying alumina, Al2O3, but mica-glass tape was absolutely needed.

The winding of a coil layer is shown in Fig. 4.10. The insulated cables were wound under a tension of 500 N for the inner layer and about 300 N for the outer layer. After winding, each single-layer coil with its clamping and confining fixtures (Fig. 4.11) was placed in the reaction oven where the following operations were carried out: (1) evacuation at room temperature; (2) heating up to 600 °C in an argon atmosphere; (3) firing at 600 °C with dry air circulation for about half an hour in order to eliminate the organic component of the insulation; (4) evacuation; (5) heat treatment at 675 ° C under flowing argon for about 140 h; (6) slow cool-down to room temperature under an argon atmosphere. The end view of a reacted coil inner layer is shown in Fig. 4.12.

Fig. 4.10
figure 10

Winding a coil layer. (Courtesy of ELIN, Austria)

Fig. 4.11
figure 11

A coil layer ready for reaction clamped by stainless-steel tooling blocks. (Courtesy of ELIN, Austria)

Fig. 4.12
figure 12

End view of a reacted coil inner layer. (Courtesy of ELIN, Austria)

After reaction, an inter-layer insulation sheet (Nomex®, DuPont, USA) was placed around the inner layer, the two coil layers were assembled, and the internal Nb3Sn-Nb3Sn splice between the inner and outer layers was made. The making of the splice, placed in the straight part of the coil, can be described as follows: during winding, the first turn of the inner layer is bent (the jump) to reach the level of the outer layer where it continues straight for about 250 mm (about two transposition lengths). The corresponding part of the outer layer cable first turn, also about 250 mm long, remains straight in its normal place. The soldering of the two corresponding parts is made by inserting between them a Pb60Sn40 foil, and then performing a pressing and heating operation. Two voltage taps are then soldered to the splice. For additional stability, the splice is then inserted and soldered in a U-shaped copper piece, which is insulated and lodged in a slot in the central post.

After placing the central post, the Nb3Sn-Nb-Ti splices of the coil terminals were also made using Pb60Sn40 solder. The coil-to-ground insulation (Nomex®) was wrapped around the coil, which was then placed in the impregnation mold, whose closing plate was tightened by bolts with a force of 600 kN in order to apply a tangential compression of about 10 MPa to the windings.

After evacuation, impregnation with epoxy resin and curing were performed with a similar resin and procedure that had been used in the CERN ISR superconducting quadrupoles (Billan et al. 1976): Ciba-Geigy, Switzerland resin system composed of Araldite MY745 (100 pbw) epoxy, HY905 hardener (100 pbw), and DY072 (1 pbw) and DY073 (0.2 pbw) accelerators. The impregnation was performed for 8 h at 90 °C and a curing cycle for 24 h at 120 °C.

After impregnation, the coil was extracted from the mold, cleaned of resin and demolding agent residues, and replaced into the mold to measure its elastic modulus. Measurements were made in the central part of the coil over 100 mm, paying attention not to introduce shear. After some pressing cycles to verify the reproducibility of force vs. displacement behavior, the E modulus was measured at pressures of around 50 MPa: the result for the coil azimuthal E modulus was about 28 GPa. This value was in relatively good agreement with the E measured on cable stacks (see Sect. 4.5.2). This result was used to determine the thickness of the shims inserted between the coils in the magnet median plane to obtain the pre-stress required at collaring.

The two coils were then assembled, and the collars were placed around them. After some pressing cycles to settle the assembly, the collars were pressed to the prescribed force and the locking keys inserted.

The yoke halves were then mounted with a slight compression, sufficient to guarantee integrity of the assembly during handling, and provisionally kept in place with belts. The stiff end plates were fixed to the tie rods. Finally, the outer aluminum alloy cylinder was shrink-fitted by warming it up to 200–250 °C. An insulating plate to support the external connections was fixed to the magnet end plates. The two coils were then soldered together with two Nb-Ti cable terminals and the lead Nb-Ti cables were fixed to their support.

7 Mirror Coil Test Facility

A 1 m long, 5 cm diameter half-bore mirror dipole was built at ELIN to test single coils. Its cross-section is shown in Fig. 4.13. In the mirror dipole, one coil is replaced by an iron insert. In this set-up no collars were used: the necessary pre-stress on the coil is provided by the yoke halves surrounded by the aluminum shrinking cylinder.

Fig. 4.13
figure 13

Simplified cross-section of the Mirror Test Facility: 1 – coil; 2, 3 – central post parts; 4 – copper shield; 5 – iron mirror; 6 – iron yoke; 7 – shrinking cylinder

8 Tests and Performance

The magnet prepared for installation in a Dewar is shown in Fig. 4.14. At various steps of magnet construction, voltage taps were placed: at the coil inter-layer splices, at the coil Nb3Sn/Nb-Ti terminal splices, and at the magnet leads. All voltage taps were doubled for redundancy, so in total 12 voltage taps were installed. An elaborate protection system, with heaters for rapidly quenching the entire magnet, was not necessary for this short magnet and, therefore, not installed. Of course, for longer magnets such a system would be mandatory.

Fig. 4.14
figure 14

The magnet ready to be inserted into a vertical cryostat for tests. (Courtesy of CERN)

In this short model magnet, protection was ensured by two resistors inserted in the circuit. One resistor was placed across the magnet leads inside the cryostat, to provide protection in case one or both cryogenic current leads failed. The second resistor was placed outside the cryostat and was normally short-circuited by a circuit breaker. When a quench was detected (by comparing voltages across the two coils), the circuit breaker was opened, thus forcing the magnet current through the two resistors.

An early coil, mounted in the Mirror Coil Test Facility, had been tested in February 1989. It reached a central field of 10.2 T at 17,430 A, 4.3 K, after eight quenches (Fig. 4.15). The magnetic field was measured by means of a Hall plate magnetometer. After full thermal cycle, the same field was attained without retraining. When tested at 1.9 K the quench field was the same, an indication that the mechanical limit was reached. All quenches started in the inner layer of the coil.

Fig. 4.15
figure 15

Quench history of the mirror (half-dipole) at 4.3 K

The full magnet was tested in June 1989. It reached a central bore field of 9.5 T at a current of 15,600 A at 4.3 K, corresponding to about 10.05 T in a turn of the inner layer. Thermal cycling to room temperature did not affect the field level and negligible retraining occurred (Fig. 4.16). As in the mirror configuration, all quenches started in the inner layer of the coils. The field attained in the dipole model was slightly lower than in the mirror configuration due to the lower Nb3Sn content in the dipole inner-layer cable and the larger distance to the iron yoke.

Fig. 4.16
figure 16

Quench history of full dipole at 4.3 K

9 Coil with Powder-in-Tube Cables

Upon delivery of the prototype cable lengths, a coil was manufactured by ELIN and mounted in the Mirror Coil Test Facility. Its construction followed the same procedure as the previous bronze route coils. It was tested in December 1991. The central field reached at the first quench was 7.43 T at a current of 11,270 A at 4.3 K, a remarkable result for a first experimental production of a novel conductor. More than 20 excitations were made. At small ramp rates up to 100 A/s all quenches happened at the same field level, about 7.4 T. A possible explanation could be that they were caused by a localized defect in a conductor. Higher ramp rates affected the quenching field: 7.1 T at 200 A/s, 6 T at 250 A/s, and 5 T at 300 A/s. This could be due to the large Nb3Sn filament size.

This was the last construction activity at that time at CERN on the Nb3Sn option, as all CERN resources had to be concentrated on the Nb-Ti line. In Europe activity on Nb3Sn magnets continued, with CERN’s involvement, by a collaboration with the Netherlands Institute for Nuclear & High Energy Physics (NIKHEF), the Netherlands Foundation for Fundamental Research on Matter (FOM) and the University of Twente. This culminated in the successful construction of the Model Single of the University of Twente (MSUT) dipole model, which was tested at CERN in 1995, reaching 11.03 T at 4.4 K at its first quench.

10 Conclusion

In 1989 the CERN–ELIN model magnet made a real breakthrough in accelerator magnet technology. A moment of celebration of this success is shown in Fig. 4.17. It was the first successful dipole of particle accelerator type made with Nb3Sn superconductor. It reached record field levels of 9.5 T in the full dipole and 10.2 T in the magnetic mirror configuration. Its design and fabrication were in an industrial style, showing that the Nb3Sn option was a realistic one for attaining field levels not accessible to Nb-Ti. Considerable technological advancement was achieved, in particular concerning the electrical insulation of the cables, the coil winding, and the reaction process. The manufacturing of the coil was, however, complicated and delicate, requiring maximum attention at all steps.

Fig. 4.17
figure 17

Project leaders congratulate the team for the successful magnet test (17 June 1989)

It was recognized that important improvements were necessary to obtain better performing and less stiff conductors. The development of processes other than the bronze route such as jellyroll and PIT, still in their initial phases, had to be strongly supported because they promised higher current density and easier winding. One key challenge for PIT process development for use in particle accelerators was towards smaller filaments.

The cable insulation also needed great improvements in mechanical strength, flexibility, and resistance to high temperatures. At that time there was a consensus that insulation materials other than mica and glass should be investigated, for instance ceramics. These improvements on the basic materials, superconductors, and insulation, would lead to safer and more economical coil fabrication.

In 1991 CERN decided to adopt Nb-Ti for the LHC magnets, and consequently all CERN resources had to be concentrated on developing this technology. This decision was taken after thorough discussions at all levels. It was based on the following main arguments:

  • The technology of Nb3Sn superconductors was still in an experimental stage, while Nb-Ti was an industrial product manufactured and commercialized at market prices by several companies.

  • Only one Nb3Sn accelerator type short magnet and none of the length required for the LHC (10 m or more) had successfully been built.

  • The cost of Nb3Sn magnets was estimated to exceed by far the foreseen budget.

  • Industrialization of superfluid cryogenics was deemed easier to achieve, less expensive, and less risky than that of Nb3Sn magnets.